Here is a list of all the postings Les Jones 1 has made in our forums. Click on a thread name to jump to the thread.
Thread: chinese lathe tailstock is 3/16" too high |
10/08/2021 10:41:03 |
If the headstock is removable from the bed would it be possible to make a packing piece to raise the headstock by 3/16" ? Les. |
Thread: Spotting through, Drilling through & which order |
03/08/2021 15:50:57 |
When drilling the holes in the cylinder cover do not drill them to the final size. (Screw clearance size.) Drill them to the tapping hole size. (Or smaller.). Les. |
Thread: Is there a chart for drill hole dia vs. boring bar size? |
24/07/2021 09:26:34 |
You seem to be assuming that the cutting tip is level with the top surface of the boring bar. If you make your boring bar with the cutting tip close to the centre line of the boring bar then the diameter of the main part of the boring bar can be closer to the starting hole size. Les. |
Thread: 12 volt motor speed controller |
19/07/2021 11:57:50 |
Can you provide some information on the board ? As a TOTALLY WILD GUESS there is probably a power mosfet that does the switching of the motor current. Using a switch to short source and drain should work. (The switch will have to carry the full motor current.) Les. |
Thread: Spiral Milling |
16/06/2021 18:24:45 |
I did a similar thing using a a rotary table and a right angle drill adapter.
Les. |
Thread: DIY Hydraulic Press |
10/06/2021 22:31:44 |
Is it not possible to draw them in using threaded rod, short lengths of tube and some thick washers ? It is over 50 years since I had an A series engine in bits so my best best guess would be that 6mm is about the largest threaded rod that would fit through the valve guides. Les. |
Thread: DRO Question |
28/05/2021 20:21:17 |
I agree with chrisB that your scales are the capacitive type and they will not work most display units as most of them expect quadrature signals which most glass(Optical) and magnetic scales provide. To make things more complicated there are a number of different protocols used with capacitive scales. There is one DIY design that works with some types of capacitive scales. This is a link to it. I have not followed that project for a few years so I don't know the capabilities of the current version. Les.
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Thread: Loctite or Draper? Much difference? |
11/04/2021 20:45:57 |
If you are planning to use it to try to remove the bearing I think it is not the correct grade. For that i suggest 638 Les. |
Thread: How do I remove this small bearing? And the one behind it. |
10/04/2021 14:37:34 |
The grade of loctite that I have used in the past is 638. Les. |
10/04/2021 10:58:54 |
Try turning down the end of some threaded rod (10mm or above.) to a couple of thou under 8mm. Clean out any oil or grease from the hole in the bearing. Loctite the end of the threaded rod into the bearing and leave it for a day or so to set. Use a suitable length of tube and thick washer to draw the beating out. (I can't remember which grade of loctite is the strongest.) You can remove the threaded rod from the bearing using heat, Repeat the process for the second bearing. Les. Edited By Les Jones 1 on 10/04/2021 10:59:37 |
Thread: Noise from Crompton Parkinson 3 phase 1/2 HP motor |
05/04/2021 17:39:00 |
Although Howard's comment about slip rings is wrong (As it will not have slip rings) It made me wonder if it's 3 phase supply was derived from a static converter rather than being a true 3 phase supply. If it was then that MAY have some influence on the problem. Les. Edited By Les Jones 1 on 05/04/2021 17:39:39 |
05/04/2021 15:58:04 |
You could try covering the rotor with engineer blue or a marker pen then run the motor in the direction that gives the noise. After it has run for a time you could examine the rotor to see if any of the marker has been rubbed off. Les. |
Thread: strange 240v pump 'switching' |
04/04/2021 12:36:09 |
I think Stuart Smith is probably thinking along the right lines. A thermal cut out (Or an intermittent connection inside the pump.) seems likely. It probably warms up and the contact breaks. It then cools down and the contact re makes. Les. Edited By Les Jones 1 on 04/04/2021 12:36:34 |
Thread: Tyre Guage DRO - capacitance issues? |
03/04/2021 13:16:27 |
Looking at your picture it looks like the casing is all plastic. I think connecting one side of the battery connections to the mill metal work may solve the problem. Just in case there is already some connection via metalwork that I can't see I suggest making the connection via a capacitor. I suggest about 100 nF but the value is not critical. Also it should not matter which battery connection you connect to. I think there is a removable cover to connections for a remote readout to the right of the battery cover. (As positioned in your picture.) There will be 4 connections. two connect to the battery. (You can check which these are with a DMM on the resistance range.) The other two connections will be data and clock signals. The battery connections under this cover are probably the easiest to make a connection to. Les. |
Thread: Steel tube for sand muller |
31/03/2021 10:20:39 |
Possibly a rear roller from a cylinder type lawn mower. Les. |
Thread: Domestic water hammer |
24/03/2021 14:45:27 |
Are the taps that give the problem fed from the high pressure mains supply that feeds the tank or are they fed from the output of the tank ? Assuming they are fed from the high pressure side it may be that the new ball valve has a snap action cut off rather than the type that gradually shuts off the flow into tank. I think Jon Lawes about air in the pipes acting as a cushion before the ball valve was replaced could be right. If so fitting a Hammer Arrester may solve the problem. (Search Toolstation, Screwfix, or plumbing suppliers for " Hammer Arresters" to find one.) Les.
Hammer Arresters
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Thread: Invertek Optidrive Control Issue |
08/03/2021 10:59:32 |
From the link that old mart has provided check that you have set the parameters in table 11.1 on page 11 correctly. Les. |
Thread: mitre saw use for roughing out/ vertical milling mild steel? |
05/03/2021 15:47:37 |
If the saw blade was 80mm diameter then for the same cutting force the torque required would be 20 times as much as required for a 4mm diameter end mill. So if the saw blade was 2mm thick it would be like a 2mm depth of cut with a 4 mm end mill. I don't think I would attempt a 2mm depth of cut using a 4mm end mill on steel. To use the same motor you would need to gear it down by a ratio of 20:1 to increase the torque by 20:1 Les. Edited By Les Jones 1 on 05/03/2021 15:49:42 |
Thread: Battery Packaging Teaser |
24/02/2021 11:08:14 |
When I was working I ordered some 2032 (Or similar cells.) though the companies logistics system. when I opened the package I found they had been packed in anti static bags. And as I expected they were all totally flat. A good example of a rule being made to protect things being use without applying common sense. Les. |
Thread: Warco wm250 - wiring issue |
21/02/2021 18:03:30 |
I agree with Oldiron that you should start your own thread. Also I seem to remember seeing information on three versions of the WM250 One uses a fixed speed single phase induction motor. Another uses a DC motor with a speed controller and yet another uses a three phase motor driven by a VFD. It would help it you tell us which version you have. Put that information in the first post of your new thread. Les. |
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