Robert Dodds | 27/11/2021 21:51:55 |
324 forum posts 63 photos | OK Steve,
Get your slots uniform in size and round particularly at the nut closed position. then produce two pins of a diameter to suit your slot size less 0.002" to 0.005"and get the thread as concentric as possible . I would remove shims at initial tryout as I doubt that it left the factory with shims. After all they cost less than £20 in the thirties so didn't get much individual attention. Regards Bob D Edited By Robert Dodds on 27/11/2021 21:56:25 |
Howard Lewis | 28/11/2021 06:55:13 |
7227 forum posts 21 photos | Robert has confirmed what I suspected, that the 3/16 pins were a later, incorrect, modification. The problem with any pre owned machine, particularly a really old one, is that there is little way ofknowing what incorrect modification shave been done. The half nuts jumping out, probably caused by the incorrect pins being fitted, may be the reason why the lathe was sold, Getting it back to original specification, as closely as possible, has to be the first step along the road to correct operation. With regard to Leadscrew alignment, may i suggest the following as means of effecting an improvement? (Having made two new 1/4" diameter pins, with 3/16 BSW threads, hopefully the half nuts will engage satisfactorily. ) 1 ) Slacken the bolts retaining the Leadscrew bearings at both ends of the bed. This will allow the Leadscrew to move in the vertical plane. 2 ) Move the Saddle to the Headstock end and engage the half nuts. It may be necessary to rock the chuck to and fro to obtain engagement. 3 ) Tighten the bolts 4 ) Disengage the half nuts, and move the Saddle to the Tailstock end. 5 ) Engage half nuts. 6 ) Tighten bolts. Disengage half nuts and recheck Leadscrew alignment measurements. Hopefully they will now be more alike! This may be the time to reshim the Apron to ensure optimum alignment with the Leadscrew. These processes might need to be repeated to get the best fit and operation. If the banjo is tight to move, that is another problem to investigate and solve, but AFTER the above has been completed and finalised., without any further movement of the Leadscrew bearings! Eliminate one problem at a time, or you will merely confuse matters and not know what is causing what. Howard Edited By Howard Lewis on 28/11/2021 06:55:49 Edited By Howard Lewis on 28/11/2021 06:56:35 |
Steve355 | 28/11/2021 09:22:28 |
321 forum posts 235 photos | Posted by Howard Lewis on 28/11/2021 06:55:13:
Robert has confirmed what I suspected, that the 3/16 pins were a later, incorrect, modification. The problem with any pre owned machine, particularly a really old one, is that there is little way ofknowing what incorrect modification shave been done. The half nuts jumping out, probably caused by the incorrect pins being fitted, may be the reason why the lathe was sold, Getting it back to original specification, as closely as possible, has to be the first step along the road to correct operation. With regard to Leadscrew alignment, may i suggest the following as means of effecting an improvement? (Having made two new 1/4" diameter pins, with 3/16 BSW threads, hopefully the half nuts will engage satisfactorily. ) 1 ) Slacken the bolts retaining the Leadscrew bearings at both ends of the bed. This will allow the Leadscrew to move in the vertical plane. 2 ) Move the Saddle to the Headstock end and engage the half nuts. It may be necessary to rock the chuck to and fro to obtain engagement. 3 ) Tighten the bolts 4 ) Disengage the half nuts, and move the Saddle to the Tailstock end. 5 ) Engage half nuts. 6 ) Tighten bolts. Disengage half nuts and recheck Leadscrew alignment measurements. Hopefully they will now be more alike! This may be the time to reshim the Apron to ensure optimum alignment with the Leadscrew. These processes might need to be repeated to get the best fit and operation. If the banjo is tight to move, that is another problem to investigate and solve, but AFTER the above has been completed and finalised., without any further movement of the Leadscrew bearings! Eliminate one problem at a time, or you will merely confuse matters and not know what is causing what. Howard Edited By Howard Lewis on 28/11/2021 06:55:49 Edited By Howard Lewis on 28/11/2021 06:56:35 That makes a lot of sense Howard. The thing that’s perplexing me though, is that there is no adjustment at the tailstock end - the support for the lead screw is cast into the bed. There is adjustment at the headstock end, but I unbolted it last night, but surprisingly the amount of adjustment available was very, very limited. Maybe 1mm of play up and down, essentially the play in the holes that hold the bolts. I was able to lift it slightly and re-bolt it, which seemed to place the lead screw parallel with the bed, as confirmed by a depth gauge. I came to the conclusion that the adjustment available was only to enable the lead screw and bed to be parallel, and the vertical placing of the half nuts was done by shimming the apron. Or something else, but I’m running out of ideas! Pic shows the bolts I unscrewed,
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Steve355 | 28/11/2021 09:34:33 |
321 forum posts 235 photos | Posted by Robert Dodds on 27/11/2021 21:51:55:
OK Steve,
Get your slots uniform in size and round particularly at the nut closed position. then produce two pins of a diameter to suit your slot size less 0.002" to 0.005"and get the thread as concentric as possible . I would remove shims at initial tryout as I doubt that it left the factory with shims. After all they cost less than £20 in the thirties so didn't get much individual attention.
Regards Bob D
Bob, Thanks very much for the suggestion. I have filed out the slots. I don’t have any letter drills but a 6mm drill bit seemed to be a sensible option, and so I have filed it so the bit is snug but runs freely throughout the length of the slot. They were not at all even or consistent previously. Next step, make up a couple of 6mm pins with 3/16” threads on the end. I will probably go to hell for making a metric modification to an old imperial lathe, but needs must I suppose. Cheers Steve |
John Hinkley | 28/11/2021 10:05:12 |
![]() 1545 forum posts 484 photos | Posted by Steve355 on 28/11/2021 09:34:33:
Next step, make up a couple of 6mm pins with 3/16” threads on the end. I will probably go to hell for making a metric modification to an old imperial lathe, but needs must I suppose. Cheers Steve If you want to avoid the trip to hell, make the pins 0.236 inch diameter! Imperial and metric are only different ways of expressing the same thing. As for your threading problem, to make the new pins, a temporary solution might be to keep the nuts engaged and wind the cross slide back under power or by hand, if your chuck screws on. John
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Robert Dodds | 28/11/2021 13:05:04 |
324 forum posts 63 photos | Steve, In making those 6mm pins do make sure that the 3/16" thread is concentric as possible with the 6mm O/D. As a last resort to avoid shims on the Apron the 6mm pins could intentionally be made eccentric to the threaded portion and thereby vary the engagement position of the half nuts, but that's not for the faint hearted. |
Robert Dodds | 28/11/2021 15:58:17 |
324 forum posts 63 photos | Steve, Will your 6mm rod pass through the vertical slots in the apron or are they designed for 3/16" rod.in which case you will need to make them look like cheese head screws. Reference the symmetry I wrote about, check the two dimensions indicated on your edited photo and see if they are near equal. They will determine which of your half nuts moves most when you rotate the "banjo" Bob D |
Steve355 | 29/11/2021 21:39:59 |
321 forum posts 235 photos | Here we go…l
So….. it feels much more solid and decisive. It hasn’t skipped at all. Much better. This is a .236” (as suggested) pin with the end turned down further to 3/16 for the thread into the half nut. it does still flex the lead screw upwards slightly as it engages. Not sure why - might be because I haven’t got the measurement Bob pointed out quite right. Or something. I will try to cut a thread before work tomorrow. Right now I need a rest from the damn thing!
Edited By Steve355 on 29/11/2021 21:41:25 Edited By Steve355 on 29/11/2021 21:42:00 |
Howard Lewis | 30/11/2021 06:20:29 |
7227 forum posts 21 photos | Steve, That looks more hopeful You have a PM Howard |
Steve355 | 30/11/2021 08:55:50 |
321 forum posts 235 photos | Looking much more hopeful… |
ega | 30/11/2021 11:45:48 |
2805 forum posts 219 photos | Steve355: Congratulations on your success! When you are rested, do consider making some soft clams for your vice. |
Howard Lewis | 30/11/2021 18:07:21 |
7227 forum posts 21 photos | Persistence pays off! Hurrah! Howard
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Steve355 | 30/11/2021 19:08:22 |
321 forum posts 235 photos | Posted by Howard Lewis on 30/11/2021 18:07:21:
Persistence pays off! Hurrah! Howard
Thanks Howard and thanks for all your advice. 😎 Steve |
Howard Lewis | 01/12/2021 15:32:09 |
7227 forum posts 21 photos | Hi Steve! Only too glad if I have been of any assistance. Isn't it marvelous when, after all the work and frustration, it all goes back together and works as you want! Definitely Job Satisfaction. Howard |
Steve355 | 02/12/2021 00:17:06 |
321 forum posts 235 photos | 7/8 9 TPI BSW in steel Unfortunately it’s not 7/8” cos I had to start again and turn off the first thread, but once I’d solved the problem (play in lead screw) it started working properly. But very nearly right, getting better every time. It actually holds a 7/8 nut albeit rather sloppy. Edited By Steve355 on 02/12/2021 00:19:26 |
Ronald Morrison | 02/12/2021 12:08:55 |
98 forum posts 4 photos | Posted by Steve355 on 29/11/2021 21:39:59:
it does still flex the lead screw upwards slightly as it engages. Not sure why - might be because I haven’t got the measurement Bob pointed out quite right. Or something. I will try to cut a thread before work tomorrow. Right now I need a rest from the damn thing! Check that that engaging the half nuts flexes the lead screw the same at both ends. It may be that the bearing on the outboard end needs to have its mount adjusted so the lead screw is parallel to the bed. |
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